NTSB CAROL · Event
Event WPR25FA153
Registry · N342H
FAA Aircraft Registry record.
Make / Model
AMERICAN CHAMPION AIRCRAFT 7GCBC
Year of manufacture
1998 · 27 years old at event
Engine
LYCOMING 0-320 SERIES (180 hp)
Seats / Engines
2 seats · 1 engine
Last airworthiness date
19980724
ADS-B equipped
Yes — Mode-S A3C56B
Registrant of record
TRAUTMAN MICHAEL
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Factual narrative
On May 9, 2025, about 0900 mountain daylight time, an American Champion Aircraft 7GCBC, N342H, was substantially damaged when it was involved in an accident near Big Creek, Idaho. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. According to a family member, the pilot was a hunter and had flown to many of the remote air strips around the area for pleasure. A witness located at the Big Creek airport (U60), Big Creek, Idaho, stated he observed the airplane land at the airport early that morning, and then heard the airplane take off to the north soon after. The witness did not observe the takeoff but did recall the engine sounded normal when the airplane departed. There were no known witnesses to the accident sequence. Examination of the accident site revealed that the airplane impacted heavily wooded sloping mountainous terrain about 2,000 ft north of the departure end of runway 01. The airplane came to rest upright on a heading of about 200° magnetic at an elevation of 5,538 ft. mean sea level (msl). The debris path was oriented along a heading of about 010° magnetic and was about 90 ft in length. The first identifiable point of contact (FIPC) was a series of damaged trees, about 50 ft in height, that had damaged limbs near the top of the trees. The right-wing tip was observed about 10 ft north of the FIPC. Debris extended throughout the heavily wooded area to the main wreckage. Examination of the main wreckage revealed that both wings and empennage remained attached to the fuselage. The engine remained attached to the engine mount, however, was displaced downward about 15°. The instrument panel was impact damaged and separated from the fuselage structure. The right main landing gear was separated from the fuselage and was located within the debris path. All major structural components of the airplane were located throughout the wreckage debris path. The wreckage was recovered to a secure location for further examination. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_2025_WPR25FA153.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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