NTSB CAROL · Event
Event ANC14LA071
Registry · N93E
FAA Aircraft Registry record.
Make / Model
DEHAVILLAND DHC-2 MK. I(L20A)
Year of manufacture
1956 · 58 years old at event
Engine
NONE NONE
Seats / Engines
8 seats · 1 engine
Last airworthiness date
19870213
ADS-B equipped
Yes — Mode-S ACE3B4
Registrant of record
ZVI LLC
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
The loss of engine power during takeoff due to a malfunction of the engine-driven fuel pump.
Factual narrative
On August 31, 2014, about 1800 Alaska daylight time, a deHavilland DHC-2 "Beaver" airplane, N93E, was substantially damaged during a collision with trees and terrain following a loss of engine power during takeoff from Lake Hood Strip, Anchorage, Alaska. Of the four people on board, one passenger received minor injuries and the private pilot and two additional passengers were not injured. The flight was being operated as a visual flight rules (VFR) personal flight under the provisions of 14 Code of Federal Regulations Part 91 when the accident occurred. Visual meteorological conditions prevailed and no flight plan was filed for the flight destined for a hunting camp approximately 30 miles west of Anchorage. In a written statement to the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) following the accident, the pilot stated he was making a second trip to camp that day when the engine lost power after takeoff at an altitude of about 100 feet above ground level. He unsuccessfully attempted to restart the engine, and made a forced landing in an area of densely populated spruce trees. During the forced landing the airplane sustained substantial damage to the fuselage, wings, and horizontal stabilizer. The engine and airframe were examined by the NTSB IIC at the facilities of Alaska Aircraft Sales on September 4. No airframe anomalies were noted that would have precluded normal operation. The engine was examined, and all the internal components were intact and functional. The magnetos, carburetor, and engine driven fuel pump were removed from the engine for further examination. On December 4 and again on January 14, 2015, the NTSB IIC, along with another NTSB investigator examined the removed engine accessories at the facilities of Alaskan Aircraft Engines. The magnetos and carburetor were tested with no anomalies noted. The engine driven fuel pump was tested on two separate test benches, and run through a variety of RPM/Fuel Flow/Fuel Pressure tests. Fuel flow results from the various tests revealed widely inconsistent flow rates under the same test conditions. A control fuel pump was also tested on the same equipment, with consistent results in fuel flow. The pump was disassembled and several anomalies were noted. The spline driver oil seal on the spline driver shaft was split, and was protruding through the opening in the spline driver thrust washer. The engine oil seal was not found inside the pump. It is unknown if the engine oil seal was installed, or if the ring itself deteriorated inside the housing. The overall appearance of the seal housing and pump bearings were dirty and numerous pieces of foreign matter were noted within the seal and pump housing. The fuel pump was installed on the airplane on November 1, 2000, and the engine had accrued about 520 hours of operation since the install. The pilot reported that, just after takeoff while the airplane was about 100 ft above ground level, the engine lost all power. He attempted to restart the engine but was unsuccessful. He subsequently made a forced landing in an area of densely populated trees. During postaccident bench testing, the engine-driven fuel pump produced widely inconsistent fuel flow rates. Disassembly of the pump revealed that the oil seal on the spline driver shaft was split and that it was protruding through the opening in the thrust washer. The engine oil seal was not found inside the pump. It could not be determined whether the seal had ever been installed or if the seal had deteriorated inside the housing. The seal housing and pump bearings were dirty, and numerous pieces of foreign matter were noted within the seal and pump housing. Based on the evidence, it is likely that the fuel pump malfunctioned and caused a disruption of adequate fuel to the carburetor, which resulted in a loss of engine power. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- C Aircraft-Aircraft power plant-Engine fuel and control-Fuel pump-Malfunction - C
Verbatim from NTSB's published report. Source file
NTSB_2014_ANC14LA071.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
- NASA NTRS 2026 · Conference Paper
Computational Analysis of Steady State Aerodynamics of Transonic Truss-Braced Wing Configuration in Deep Stall
This study presents a computational investigation of steady state aerodynamics of the Subsonic Ultra-Green Aircraft Research (SUGAR) Transonic Truss-Braced Wing (TTBW) configuration over a wide range …
- arXiv 2023 · arXiv preprint
Automating Bird Diverter Installation through Multi-Aerial Robots and Signal Temporal Logic Specifications
This paper tackles the task assignment and trajectory generation problem for bird diverter installation using a fleet of multi-rotors.
- arXiv 2023 · arXiv preprint
Variation of Critical Crystallization Pressure for the Formation of Square Ice in Graphene Nanocapillaries
Two-dimensional square ice in graphene nanocapillaries at room temperature is a fascinating phenomenon and has been confirmed experimentally.
- arXiv 2023 · arXiv preprint
Polycrystallinity enhances stress build-up around ice
Damage caused by freezing wet, porous materials is a widespread problem, but is hard to predict or control. Here, we show that polycrystallinity makes a great difference to the stress build-up process…
- arXiv 2022 · arXiv preprint
Enhanced Prediction of Three-dimensional Finite Iced Wing Separated Flow Near Stall
Icing on three-dimensional wings causes severe flow separation near stall. Standard improved delayed detached eddy simulation (IDDES) is unable to correctly predict the separating reattaching flow due…
- Embry-Riddle Scholarly Commons 2021 · Journal article (JAAER)
Analysis on the Negative Emotional, Physiological, and Cognitive Responses Elicited from of the Activation of a Stall Alarm
Failing to identify an aerodynamic stall can lead to the inability of an aircraft to sustain flight. To warn pilots of an impending or fully-developed stall, many aircraft have safety devices installe…
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