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Atlas / NTSB / ATL89IA187

NTSB CAROL · Event

Event ATL89IA187

1989-08-02 GREENSBORO, North Carolina, United States Airport · GSO None 1 aircraft Status: Completed

Registry · N413US

FAA Aircraft Registry record.

Make / Model

CESSNA 305A

Seats / Engines

2 seats · 1 engine

ADS-B equipped

Yes — Mode-S A4E118

Registrant of record

STOECKLEIN EDMUND H

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

FAILURE OF THE LINE MECHANIC, A CHECK MECHANIC, AND FIRST OFFICER TO IDENTIFY AND REMOVE THE WHEEL CHOCK FROM THE WHEEL WELL DURING THE REQUIRED INSPECTIONS.

Factual narrative

DURING APPROACH TO CHARLOTTE, THE MAIN GEAR WOULD NOT EXTEND. THE FLT DIVERTED TO GREENSBORO. THE RIGHT GEAR EVENTUALLY EXTENDED AFTER APPLYING EXTENSIVE G-FORCES, BUT THE LEFT GEAR WOULD NOT. AFTER LANDING, A 29-INCH WHEEL CHOCK WAS FOUND WEDGED BETWEEN THE RADIUS OF THE LEFT WHEEL WELL AND THE INBOARD WHEEL WHICH PREVENTED THE LEFT GEAR FROM FALLING DOWN. THE AIRPLANE HAD BEEN POSITIONED SEVERAL TIMES THE NIGHT BEFORE, AND THE MECHANICS RECALLED PLACING THE CHOCKS IN THE WHEEL WELL. AN A-CHECK, AND A WALK-AROUND INSPECTION, HAD BEEN COMPLETED PRIOR TO THE FLIGHT'S DEPARTURE FROM WASHINGTON. EACH INSPECTION REQUIRED AN INSPECTION OF THE WHEEL WELL AREA. THE FIRST OFFICER STATED THAT HE DIDN'T SEE THE CHOCK WHICH WAS MARKED WITH YELLOW REFLECTIVE TAPE. A FLASHLIGHT WAS USED DURING THE INSPECTION. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1989_ATL89IA187.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.