Skip to content

Atlas / NTSB / CEN18LA246

NTSB CAROL · Event

Event CEN18LA246

2018-06-30 Baldwin City, Kansas, United States Airport · K64 None 1 aircraft Status: Completed

Registry · N107BL

FAA Aircraft Registry record.

Make / Model

CESSNA 337F

Year of manufacture

1970 · 48 years old at event

Engine

CONT MOTOR IO-360 SER (300 hp)

Seats / Engines

6 seats · 2 engines

Last airworthiness date

19701124

ADS-B equipped

Yes — Mode-S A01ED9

Registrant of record

VINLAND AERODROME INC

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The loss of hydraulic accumulator pressure for reasons that could not be determined, which prevented the propeller from unfeathering, and the pilot's improper decision to attempt a go-around, which resulted in an off-airport landing and the airplane impacting trees and a fence. Contributing to the accident was the loss of tension at the flap switch pivot, which prevented it from holding position.

Factual narrative

***This report was modified on November 7, 2019. Please see the docket for this accident to view the original report.*** On June 30, 2018, about 1155 central daylight time, a Cessna 337F, N107BL, a multiengine centerline thrust airplane, was substantially damaged when it struck trees and a fence during a forced landing about one mile southeast of Vinland Valley Aerodrome (K64), Baldwin City, Kansas. The commercial pilot was not injured. The airplane was registered to and operated by Vinland Aerodrome, Baldwin City, Kansas, under the provisions of Title 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed at the time of the accident, and no flight plan had been filed for the local personal flight. According to the pilot, who is also an airframe and powerplant (A&P) mechanic, he took off and climbed to 3,500 ft to practice single-engine operations. He shut down the rear engine and feathered the propeller. After doing some air work, the pilot attempted to unfeather the propeller and restart the rear engine but was unsuccessful. He returned to the airport and made a single-engine landing approach. During the approach, the pilot noticed [he had lost his] full flap down setting and determined a full stop landing on the grass runway was going to be close. He reduced flaps to 10°. The flap setting "relaxed" and the pilot determined there was insufficient altitude available to retract the landing gear. The pilot maneuvered to avoid houses and made a forced landing in a crosswind. Full power and full flaps were used until touchdown. The airplane struck small trees, shrubs, and a fence. The left wing was bent and the fuselage was buckled. The rear engine propeller has a remote hydraulic accumulator that assists in unfeathering the propeller and is serviced to 120 psi. During annual inspection 4 hours prior to the accident flight, it was found to be slightly low. Post-accident examination revealed the pressure to be 85 psi. It is most likely a nitrogen leakage had developed during those 4 hours. The flap switch was not holding position; the reason for this anomaly could not be determined. The commercial pilot was conducting a local flight to practice single-engine maneuvers. After taking off and climbing the airplane to 3,500 ft, he shut down the rear engine and feathered the propeller. After performing some turns and climbs, the pilot attempted to unfeather the propeller and restart the engine but was unsuccessful. He returned to the airport to set up for a single-engine approach. During the approach, the pilot realized that the flaps were no longer in the full-flap setting and that a landing on the grass runway was going to be close, so he chose to perform a go-around. However, as the pilot began to go around, he realized that the airplane could not maintain altitude. He maneuvered the airplane for an off-airport landing to a nearby field, during which the airplane struck small trees and a fence and sustained substantial damage to the left wing and fuselage.   The rear engine propeller had a remote hydraulic accumulator that assisted in unfeathering the propeller and was normally serviced to 120 pounds per square inch (psi). During an annual inspection that took place 4 flight hours before the accident flight, it was noted that the pressure was slightly low. During postaccident examination, the accumulator pressure was 85 psi. It is likely that a nitrogen leak occurred between the time the accumulator was last serviced and the time of the accident; however, the reason for the nitrogen leak could not be determined. Further, the flap switch was not holding position due to a loss of tension at the flap switch pivot, which is likely why the flaps were not in the full-flap setting as reported by the pilot. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • C Personnel issues-Task performance-Maintenance-Scheduled/routine maintenance-Pilot - C
  • C Aircraft-Aircraft power plant-Engine (reciprocating)-(general)-Malfunction - C
  • C Aircraft-Aircraft systems-Flight control system-TE flap control system-Malfunction - C

Verbatim from NTSB's published report. Source file NTSB_2018_CEN18LA246.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (go-around). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗