NTSB CAROL · Event
Event CEN19TA280
Aircraft involved
Probable cause & findings
A loss of engine power due to fuel starvation, which resulted from attitude-induced unporting of the fuel.
Factual narrative
On August 20, 2019, about 1030 mountain daylight time, a Bell 47G-3B-1, N1170W, lost engine power during aerial application near Montrose, Colorado. The commercial pilot was seriously injured, and the helicopter sustained substantial damage to the tail boom and fuselage. The helicopter was registered to and operated by Olathe Spray Service, Inc., Olathe, Colorado, as a Title 14 Code of Federal Regulations Part 137 aerial application flight. Visual meteorological conditions prevailed at the accident site and at the time of the accident, and no visual flight rules flight plan had been filed for the local flight. The local flight departed about 1000. The pilot stated that he had been performing agricultural spray operations in four different locations. He returned to Clifford Field Airport (1CO4), Olathe, Colorado, his home base, to take on additional chemical product. On the three previous trips, pesticide and about 30 gallons of Jet-A fuel were added as the helicopter sat idling. On this, the fourth trip, the helicopter was serviced with chemical, but no fuel was added. Each spray pass was performed about 85 mph and just above the crop in order to achieve optimal product application and spray coverage to the crop. In order to do this the helicopter, at that speed, was flown in a nose-low attitude. The fuel delivery port/tube on both tanks is located at the aft, lower end of each tank, and both tanks deliver fuel to the engine simultaneously. There is no pilot-controlled fuel selector valve in the cockpit. During the aerial application, the helicopter yawed left when the engine flamed out. The pilot slowed the airspeed and the helicopter impacted a cornfield. The helicopter had been resting on its right side in a corn field for several days before a Federal Aviation Administration (FAA) inspector and a representative of the engine manufacturer examined it. As a result, it could not be determined if fuel had drained out of the right fuel tank through a vent line, loose filler cap, or breached tank, but approximately 2/3 to 3/4 gallon of clean, clear, odor-free fuel was drained from of the right tank, and 2-1/2 gallons were drained from the left tank. Fuel was also found from the inlet side of the airframe-mounted fuel filter to the fuel spray nozzle inlet on the engine. The fuel spray nozzle appeared normal with no signs of excessive carbon deposits or blockage. Both the airframe and engine fuel filter bowls contained clean fuel, and both filters were void of contamination. N1 (gas producer) and N2 (power turbine) rotor continuity was confirmed, and both rotors turned smoothly when rotated by hand. Cockpit controls from the throttle and collective back to the engine fuel control unit and power turbine governor were free and continuous. The engine oil system, including the filter and magnetic plugs, was checked and was unremarkable. Further examination revealed no evidence of mechanical malfunction or pre-existing conditions that would have precluded normal engine operation. Before the pilot performed an aerial application, the helicopter was serviced with pesticide, but no fuel was added; fuel had been added before the three previous flights. During one of the aerial application passes, the engine lost power; the pilot conducted a forced landing to a field, and the helicopter’s tailboom and fuselage were substantially damaged. Following the accident, about 3/4 gallon of fuel was recovered from the right fuel tank and 2 1/2 gallons of fuel were recovered from the left fuel tank. There was no evidence of mechanical malfunction of failure that would have precluded normal engine operations. Each spray pass is made at an airspeed of about 85 mph and directly above the crop to achieve optimal product application and spray coverage to the crop. At that speed, the helicopter flies in a nose-low attitude. The fuel delivery port or tube on both tanks is located at the aft, lower end of each tank, and both tanks deliver fuel to the engine simultaneously. It is likely that the limited fuel in the tanks moved away from the fuel ports due to the helicopter's nose-low attitude, resulting in fuel starvation. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- F Aircraft-Fluids/misc hardware-Fluids-Fuel-Fluid level - F
- F Aircraft-Fluids/misc hardware-Fluids-Fuel-Related operating info - F
- F Aircraft-Aircraft systems-Fuel system-Fuel distribution-Design - F
- F Aircraft-Aircraft systems-Fuel system-Fuel distribution-Capability exceeded - F
Verbatim from NTSB's published report. Source file
NTSB_2019_CEN19TA280.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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