NTSB CAROL · Event
Event CEN20LA055
Aircraft involved
Probable cause & findings
A total loss of engine power for reasons that could not be determined based on the available information.
Factual narrative
On January 4, 2020, about 1600 central standard time, an Aero Commander 100 airplane, N5573M, sustained substantial damage when it was involved in an accident near Mullin, Texas. The student pilot and flight instructor were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight. The flight instructor reported that he and the student departed on the 75-nautical-mile flight with 40 gallons of fuel onboard. About 3 miles from the destination airstrip, they initiated a slow descent to a private airstrip. The student completed the Descent and the Before Landing checklist. About 3,000 ft above mean sea level, the engine lost total power. The instructor immediately took control of the airplane and ensured that the fuel selector switch was selected for both fuel tanks, the carburetor heat was applied, and the mixture control was at the full-rich position. He trimmed the airplane for its best glide speed and the student completed a mayday call. The instructor switched fuel tanks; however, the engine did not respond, and the propeller was “wind milling.” The instructor performed a forced landing to a flat, plowed dirt field, during which the right wingtip impacted a tree and the airplane nosed over. The airplane sustained substantial damage to the fuselage, both wings, and the empennage. The fuel system was breached during the accident and the exact amount of fuel onboard at the time of the loss of engine power could not be determined. The airplane was recovered from the accident site and an engine run was performed. The engine successfully ran for several minutes at various power settings when a fuel source was plumbed to the engine. No mechanical anomalies were found during the engine run. Examination of the fuel selector revealed that either the fuel selector handle or the pointer was installed 180° out of position. When the selector handle was selected to BOTH, the valve was completely closed, in what should have been the OFF position. When the selector handle was selected to OFF, the valve was open, in what should have been the BOTH position. The hole on the end of the pointer that slid over the shaft featured a round side and a flat side, which helps to correctly orient the pointer during installation. The hole was sufficiently worn that the pointer would fit over the shaft in both directions. The examination could not determine if the selector handle or the pointer was installed incorrectly. The temperature and dewpoint for the accident time and accident site were not conducive to the formation of carburetor icing. The flight instructor and student pilot were conducting a cross-country flight. During a gradual descent to the destination airstrip, the engine lost total power, and the airplane sustained substantial damage during the subsequent forced landing. The airplane was recovered from the accident site and an engine examination and test run revealed no anomalies. Examination of the fuel selector revealed that either the fuel selector handle or the pointer was installed 180° out of position. When the selector handle was selected to BOTH, the valve was completely closed, in what should have been the OFF position. When the selector handle was selected to OFF, the valve was open, in what should have been the BOTH position. The temperature and dewpoint for the accident time and accident site were not conducive to the formation of carburetor icing. It is possible that if the fuel selector was manipulated to the BOTH position during the flight, the fuel may have been prevented from reaching the engine due to the incorrect installation of the selector handle. However, the examination could not determine whether it was the selector handle or the pointer that was installed incorrectly. Based on the available evidence, the reason for the total loss of engine power could not be determined. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- — Aircraft-Aircraft power plant-Engine (reciprocating)-(general)-Unknown/Not determined
- — Not determined-Not determined-(general)-(general)-Unknown/Not determined
Verbatim from NTSB's published report. Source file
NTSB_2020_CEN20LA055.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (icing, stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
- NASA NTRS 2019 · Technical Memorandum (TM)
A preliminary study of a wake vortex encounter hazard boundary for a B737-100 airplane
A preliminary batch simulation study was conducted to define the wake decay required for a Boeing 737-100 airplane to safely encounter a Boeing 727 wake and land.
- NASA NTRS 2018 · Other
A Numerical Simulation Study to Develop an Acceptable Wake Encounter Boundary for a B737-100 Airplane
The National Aeronautics and Space Administration (NASA) is conducting research with the goal of enabling safe improvements in the capacity of the nation's air transportation system.
- NASA NTRS 2011 · Other
A unified cleaning facility in a Class 100 clean room
Downdraft clean room for cleaning and potting of mechanical and electrical components and various plastics systems
- arXiv 2023 · arXiv preprint
Variation of Critical Crystallization Pressure for the Formation of Square Ice in Graphene Nanocapillaries
Two-dimensional square ice in graphene nanocapillaries at room temperature is a fascinating phenomenon and has been confirmed experimentally.
- arXiv 2022 · arXiv preprint
Supercooled Droplet Icing and Self-Jumping on Micro/nanostructured Surfaces: Role of Vaporization Momentum
Phase change under reduced environmental pressures is key to understanding liquid discharge and propulsion processes for aerospace applications.
- arXiv 2022 · arXiv preprint
Enhanced Prediction of Three-dimensional Finite Iced Wing Separated Flow Near Stall
Icing on three-dimensional wings causes severe flow separation near stall. Standard improved delayed detached eddy simulation (IDDES) is unable to correctly predict the separating reattaching flow due…
Browse the full corpus — academia portal ↗