NTSB CAROL · Event
Event CEN20LA294
Registry · N1662S
FAA Aircraft Registry record.
Make / Model
RANS S-2R
Year of manufacture
1973 · 47 years old at event
Engine
P&W R1340 SERIES (600 hp)
Seats / Engines
1 seats · 1 engine
Last airworthiness date
19731030
ADS-B equipped
Yes — Mode-S A10AA7
Registrant of record
SLATER RICHARD J
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
The fatigue fracture of the upper rudder hinge that resulted in a partial separation of the rudder from the airplane during a spray pass.
Factual narrative
On July 20, 2020, at 1600 central daylight time, an Aero Commander S2-R, N1662S, was substantially damaged when it was involved in an accident near Harlan, Iowa. The pilot was uninjured. The airplane was operated as a Title 14 Code of Federal Regulations Part 137 aerial application flight. The pilot stated that, during a spray pass, he felt the airplane yaw abruptly left and remain in an uncontrollable left yaw for about 10 to 15 minutes, at times pitching uncontrollably downward. The top 2/3 of the rudder had separated and the remainder was attached. When the top portion of the rudder completely separated, the pilot regained control of the airplane and landed without further incident. The separated portion of the rudder was not recovered. The top rudder hinge had fractured through and had brown-colored features consistent with corrosion. The remaining portion of the rudder and stabilizer was retained for metallurgical examination. Postaccident metallurgical examination revealed the upper rudder hinge was fractured through the two hinge barrels attached to the vertical stabilizer aft spar. The interior surfaces of the barrels were mostly covered with a tacky black grease. Thick grease deposits were also present on adjacent surfaces above the upper barrel and below the lower barrel. Portions of the upper hinge barrel interior fracture surfaces had flat fracture features in the radial plane with curving boundaries, features consistent with fatigue. Ratchet marks were also observed consistent with fatigue emanating from multiple origins. The fatigue regions covered approximately 90% of the fractured cross-section. The vertical stabilizer was cleaned, inspected, and repaired March 8, 2011, in accordance with designated engineering approved data. Airworthiness Directive 79-10-10, To Prevent Separation of the Single Upper Hinge from The Rudder Assembly, was complied with June 3, 1997, per Federal Aviation Administration Form 337 by installing an additional rudder hinge. The pilot of the aerial application flight was spraying a field when the top portion of the rudder partially separated from the airplane. The airplane yawed abruptly left and remained in an uncontrollable left yaw for about 10 to 15 minutes, at times pitching uncontrollably downward until the broken portion of the rudder separated. The airplane landed without further incident. Postaccident metallurgical examination of the upper rudder hinge revealed a fatigue fracture. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- — Aircraft-Aircraft structures-Empennage structure-Rudder-Fatigue/wear/corrosion
Verbatim from NTSB's published report. Source file
NTSB_2020_CEN20LA294.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
- NASA NTRS 2026 · Conference Paper
Computational Analysis of Steady State Aerodynamics of Transonic Truss-Braced Wing Configuration in Deep Stall
This study presents a computational investigation of steady state aerodynamics of the Subsonic Ultra-Green Aircraft Research (SUGAR) Transonic Truss-Braced Wing (TTBW) configuration over a wide range …
- arXiv 2023 · arXiv preprint
Automating Bird Diverter Installation through Multi-Aerial Robots and Signal Temporal Logic Specifications
This paper tackles the task assignment and trajectory generation problem for bird diverter installation using a fleet of multi-rotors.
- arXiv 2023 · arXiv preprint
Variation of Critical Crystallization Pressure for the Formation of Square Ice in Graphene Nanocapillaries
Two-dimensional square ice in graphene nanocapillaries at room temperature is a fascinating phenomenon and has been confirmed experimentally.
- arXiv 2023 · arXiv preprint
Polycrystallinity enhances stress build-up around ice
Damage caused by freezing wet, porous materials is a widespread problem, but is hard to predict or control. Here, we show that polycrystallinity makes a great difference to the stress build-up process…
- arXiv 2022 · arXiv preprint
Enhanced Prediction of Three-dimensional Finite Iced Wing Separated Flow Near Stall
Icing on three-dimensional wings causes severe flow separation near stall. Standard improved delayed detached eddy simulation (IDDES) is unable to correctly predict the separating reattaching flow due…
- Embry-Riddle Scholarly Commons 2021 · Journal article (JAAER)
Analysis on the Negative Emotional, Physiological, and Cognitive Responses Elicited from of the Activation of a Stall Alarm
Failing to identify an aerodynamic stall can lead to the inability of an aircraft to sustain flight. To warn pilots of an impending or fully-developed stall, many aircraft have safety devices installe…
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