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Atlas / NTSB / CEN23FA139

NTSB CAROL · Event

Event CEN23FA139

2023-03-17 Lubbock, Texas, United States Airport · F82 Fatal 1 aircraft Status: Completed

Registry · N2061K

FAA Aircraft Registry record.

Make / Model

BEECH 58P

Year of manufacture

1978 · 45 years old at event

Engine

CONT MOTOR TSIO-520 SER (300 hp)

Seats / Engines

6 seats · 2 engines

Last airworthiness date

19780815

ADS-B equipped

Yes — Mode-S A1AAD2

Registrant of record

MILE HIGH AIR INC

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The pilot’s failure to ensure a proper fuel selector position before takeoff, which resulted in a loss of left engine power due to fuel starvation. Contributing to the accident was the pilot’s failure to maintain airplane control after the loss of left engine power.

Factual narrative

HISTORY OF FLIGHTOn March 17, 2023, about 1140 central daylight time, a Beech Baron 58P, N2061K, was destroyed when it was involved in an accident near Lubbock, Texas. The pilot sustained fatal injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. A fixed-base operator (FBO) surveillance video showed that the airplane arrived at the FBO ramp at Lubbock Executive Airpark (F82), Lubbock, Texas, about 1111. After the airplane came to a stop on the ramp, the engines were simultaneously shut down. The pilot exited the airplane, along with two adults and two children. The pilot left the ramp and later returned to the airplane about 1116 to remove baggage. A fuel truck then pulled up in front of the airplane to refuel the airplane, and the pilot again left the ramp. About 1123, fueling of the airplane was completed. The surveillance video showed the pilot walked out of the FBO building and onto the ramp toward the airplane about 1127 while holding a cell phone to his ear. He walked clockwise around the airplane while holding the cell phone, stopped behind the right wing root, then began walking in a counterclockwise direction. He stopped near the left engine while holding the cell phone and looking away from the airplane. Then he walked to the right front airplane door, which he entered about 1130. About 1131, he exited the airplane, stepped down behind the right wing, then reentered the airplane. About 1132, the left propeller began to rotate, stopped, then began to rotate again. About 1133, the right propeller began to rotate. About 1135, the airplane taxied on the ramp, and about 1136, the airplane held short of runway 35. About 1137, the airplane began its takeoff on runway 35. A witness saw the pilot of the accident airplane walk around the airplane while talking on a cell phone before the airplane’s engines started. The witness stated that he did not see or hear a run-up of the airplane’s engines before takeoff. The witness stated that the takeoff seemed like a normal takeoff. The witness stated that the airplane lifted off about 2,200 ft down the runway. Shortly after liftoff, and while the airplane was about 20-50 ft above the runway, he looked away to fill fuel from the fuel truck and then heard an audible change in engine sound. The witness then looked up at the airplane and saw it in a left bank. Another surveillance video recorded the airplane in a nose-down, left bank attitude before entering a left roll into an inverted attitude and impacting the ground. The airplane was destroyed by impact forces and a post-crash fire. PERSONNEL INFORMATIONNo pilot logbooks were recovered from the airplane. There was no record of the pilot’s flight experience or any record that the pilot met federal regulations for recency of experience. A twin-engine initial/recurrent training syllabus, dated March 14, 2023, and signed by a flight instructor, stated that the syllabus was completed using a Precision 6DOF MFD Advanced Aviation Training Device. There was no reference to federal regulations for a flight review or instrument proficiency check in this document. WRECKAGE AND IMPACT INFORMATIONThe accident site was about 0.5 nm west-northwest from the departure end of runway 35. The airplane wreckage was in a fallow and relatively flat cotton field, which was surrounded by similar fields. The major components of the airplane were accounted for at the accident site. Flight control continuity from the airplane control surfaces to the cockpit controls was confirmed. The landing gear was in the retracted position. Postaccident examination of the left and right engines revealed no preimpact mechanical anomalies that would have precluded normal engine operation. Impact forces damaged both propellers. The left propeller exhibited damage consistent with the propeller at or nearing the feathered position with low/no power. The right propeller exhibited damage consistent with rotation at higher power and at a blade angle consistent with takeoff/climb power. The left cockpit fuel selector handle sustained impact damage and was bent aft, pointing to a position between OFF and CROSSFEED. According to the aircraft manufacturer, this position is outside the normal operating range of the handle assembly. Disassembly of the left fuel selector valve assembly revealed the valve gear was in the OFF position. Continuity of the control cable was observed from the cockpit fuel selector assembly to the wing selector valve with no evidence of the cable having been pulled from impact forces. The right cockpit fuel selector handle sustained impact damage and was bent aft between the ON and CROSSFEED positions. Disassembly of the right fuel selector valve assembly revealed the valve gear was pulled beyond the OFF position by the control cable running from the assembly to the wing fuel selector valve. FLIGHT RECORDERSData download of the pilot’s personal electronics device showed that there was an incoming call at 11:28:14, before the accident. The phone call lasted 12 minutes and 34 seconds and ended at 11:40:48. The data also showed that the pilot’s phone was connected to an aviation headset via Bluetooth at 11:40:07. MEDICAL AND PATHOLOGICAL INFORMATIONAn autopsy of the pilot was conducted by the Tarrant County Medical Examiner’s Office, Fort Worth, Texas, on March 21, 2023. The autopsy report stated that the cause of death was blunt force injuries, and the manner of death was accident. The Federal Aviation Administration Civil Aerospace Medical Institute Forensic Toxicology Report for the pilot was negative for drugs of abuse. The pilot landed at the departure airport and dropped off passengers before the accident flight. The pilot then left the airplane while it was being fueled and returned after fueling was completed. The pilot walked around the airplane while talking on a cellular phone, which was not consistent with a proper preflight inspection of the airplane due to his diverted attention. After the engines were started, the airplane taxied to the departure runway. A witness stated that he did not see or hear an engine run-up before takeoff. The witness said the airplane’s takeoff was normal and later heard an audible change in engine sound after it had become airborne. Surveillance video recorded the airplane in a nose-down, left bank attitude before entering a left roll into an inverted attitude and impacting the ground. Postaccident examination of the airplane revealed that the left cockpit fuel selector was in the OFF position, which likely led to fuel starvation and a loss of left engine power. Additionally, the left engine propeller exhibited features of low/no power. The right propeller exhibited features consistent with higher power and a blade angle near takeoff/climb power. The initial left roll of the airplane likely resulted from the loss of left engine power. Examination of the engines revealed no preimpact mechanical malfunctions or failures. Flight control continuity of the airplane was confirmed and the continued left roll after the loss of left engine power indicated a loss of control by the pilot. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Personnel issues-Task performance-Inspection-Preflight inspection-Pilot
  • Aircraft-Aircraft systems-Fuel system-Fuel selector/shutoff valve-Incorrect use/operation
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Engine out control-Not attained/maintained
  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot

Verbatim from NTSB's published report. Source file NTSB_2023_CEN23FA139.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (loss of control, fuel starvation). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗