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Atlas / NTSB / ERA12LA157

NTSB CAROL · Event

Event ERA12LA157

2012-01-25 Port Orange, Florida, United States Airport · 7FL6 Minor 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

The total loss of engine power for reasons that could not be conclusively determined during postaccident examination.

Factual narrative

On January 25, 2012, about 1515 eastern standard time, a Cessna 210E, N7130U, made a forced landing following a total loss of engine power while maneuvering in the traffic pattern at the Spruce Creek Airport (7FL6), Port Orange, Florida. The airplane sustained substantial damaged and the private pilot received minor injuries. The airplane was registered to and operated by a private individual under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed and no flight plan was filed. The local flight had originated shortly before the accident. According to the pilot, it was the first flight after an engine installation and he had planned to stay in the traffic pattern. Prior to departure he conducted an engine run-up and magneto check. After everything was checked, he departed runway 5 and climbed to traffic pattern altitude of 1,000 feet. While on the downwind leg, the engine failed. He attempted to restart the engine but was unsuccessful, and attempted to return to the airport. He stated that he was too low to glide back to the field, and made a forced landing in a wooded area. Examination of the airplane by a Federal Aviation Administration inspector confirmed structural damage to the fuselage, wings, and empennage. During a cursory examination of the engine, it was noted that when the top and bottom spark plugs were removed they were packed with sand. Further examination revealed that the sand had entered through the exhaust system during recovery and entered through the exhaust system through an open exhaust valve on the No. 5 cylinder. Examination of the induction tubes revealed that the right side intake induction tube was not connected properly, the clamp was found tight but the rubber connection hose was not sealed. It was also noted that the engine was dragged out from the accident site during the recovery. In a conversation with Continental Motors it was noted that a loose intake induction tube would disrupt air flow but not necessarily cause an engine to stop. Fuel was found in the fuel injector lines going into each cylinder. Both magnetos were tested and sparked on the ignition wire towers. Examination of the magneto and ignition wiring revealed it was the original wiring and included several areas where repairs and splices had been made. During examination there was continuity in the ignition/magneto circuit; however, sections of the wiring were not sealed and insulated against grounding. No evidence of electrical arching was noted on the wiring or the surrounding engine and airframe. The fuel system was compromised from damage to the wings; however, the fuel tanks remained intact. According to the salvage company, approximately 28 gallons of fuel was removed from the fuel tanks. A sample of the fuel was inspected and no water was detected. According to the mechanics who performed the defueling, the fuel was clean and had no signs of any type of contamination. According to the pilot, it was the first flight after the engine installation. Prior to departure, he conducted a preflight engine run-up and all systems were normal. The airplane then departed and climbed to the traffic pattern altitude. While on the downwind leg of the traffic pattern, the engine failed. The pilot attempted to return to the airport but was unsuccessful and made a forced landing short of the runway in a heavily wooded area. An examination of the fuel did not reveal any contamination. While examination of the induction tubes revealed that the right side intake induction tube was not connected properly (the clamp was found tight but the rubber connection hose was not sealed), it may have become disconnected when the engine was dragged out from the accident site during recovery. Further, the engine manufacturer indicated that a loose intake induction tube would disrupt air flow but would not necessarily cause an engine to stop. Examination of the ignition system revealed that sections of the wiring were not sealed. Uninsulated or unsealed areas of the ignition system wiring could have caused grounding/shorting of the ignition system; however, the investigation was unable to conclusively determine the reason for the total loss of engine power. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • C Aircraft-Aircraft power plant-(general)-(general)-Malfunction - C
  • C Not determined-Not determined-(general)-(general)-Unknown/Not determined - C
  • Environmental issues-Physical environment-Object/animal/substance-Tree(s)-Contributed to outcome

Verbatim from NTSB's published report. Source file NTSB_2012_ERA12LA157.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗