NTSB CAROL · Event
Event LAX93LA224
Registry · N2312N
FAA Aircraft Registry record.
Make / Model
ROBINSON HELICOPTER R22 BETA
Year of manufacture
1991 · 2 years old at event
TCDS
H10WE · ROBINSON HELICOPTER CO
Engine
LYCOMING 0-320 SERIES (180 hp)
Seats / Engines
2 seats · 1 engine
Last airworthiness date
19911203
ADS-B equipped
Yes — Mode-S A20EE2
Registrant of record
HELILEASING INC
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
THE STUDENT PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL, HIS IMPROPER USE OF THE THROTTLE AND ANTITORGUE PEDALS. A FACTOR RELATED TO THIS ACCIDENT WAS THE STUDENT'S LACK OF TOTAL EXPERIENCE.
Factual narrative
On May 25, 1993 at 1920 hours Pacific daylight time, a Robinson R-22 helicopter, N2312N, collided with a fence shortly after lifting off the operator's ramp area at Whiteman Airpark (WHP), Pacoima, California. The noncertificated student pilot was beginning a local area visual flight rules solo flight. The helicopter, operated by Watson Helicopters, sustained substantial damage. The student pilot was not injured. Visual meteorological conditions prevailed. The operator reported in the Pilot/Operator Aircraft Accident Report, NTSB Form 6120.1/2, that the instructor had previously flown with the student pilot at the practice area. During the instruction period, the student performed several takeoffs and landings. The flight then returned to Whiteman Airpark. The instructor de-planed the helicopter and informed the student to make a vertical takeoff to hover, then hover over the fence and land on the end of the taxiway. The instructor observed the student make a good takeoff and hover and then walked into the building. When the student did not return to the building, the instructor walked outside and found the crash site. The student recalls the engine "RPM getting high". Witnesses observed the helicopter "swinging and yawing" prior to the tail rotor striking the ground. The student unsuccessfully tried to transition into forward flight but does not remember using the anti-torque controls to correct for the yawing effects. THE STUDENT PILOT REPORTED THAT THE ENGINE RPM WAS GETTING HIGH DURING AERIAL TAXI. WITNESSES OBSERVED THE HELICOPTER SWINGING AND YAWING DOWN THE TAXIWAY. THE STUDENT UNSUCCESSFULLY ATTEMPTED TO PUT THE HELICOPTER INTO FORWARD FLIGHT BEFORE THE TAIL ROTOR STRUCK THE GROUND. THE STUDENT PILOT DOES NOT RECALL USING THE RUDDER TO ARREST THE YAW. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_1993_LAX93LA224.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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