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Atlas / NTSB / MIA00LA220

NTSB CAROL · Event

Event MIA00LA220

2000-07-12 HARRIS, North Carolina, United States Airport · NC02 None 1 aircraft Status: Completed

Registry · N29416

FAA Aircraft Registry record.

Make / Model

AERONCA 65-TC

Year of manufacture

1940 · 60 years old at event

Engine

CONT MOTOR A&C65 SERIES (65 hp)

Seats / Engines

2 seats · 1 engine

Last airworthiness date

19590507

ADS-B equipped

Yes — Mode-S A306F0

Registrant of record

MARTIN RONALD P

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The unsuitable terrain encountered by the pilot while descending for a forced landing. Contributing to the accident was the partial loss of engine power due a blocked fuel line resulting in fuel starvation.

Factual narrative

On July 12, 2000, about 1230 eastern daylight time, a Aeronca 65-TC, N29419, registered to a private owner, collided with a wire then the ground while descending for a forced landing shortly after takeoff from the Boomerang Airport, Harris, North Carolina. Visual meteorological conditions prevailed at the time and no flight plan was filed for the 14 CFR Part 91 personal flight. The airplane was substantially damaged and the private-rated pilot, the sole occupant, was not injured. The flight originated about 1 minute earlier. The airplane was fueled with automotive fuel before takeoff from the Big Oaks Airport, and flew and landed at the Boomerang Airport. After landing, the pilot left the engine running then elected to depart. During the initial climb about 50-100 feet above ground level, the engine experienced a loss of power; insufficient power remained to sustain flight. He initiated a shallow right bank and after realizing he was unable to return to the airport, he turned towards a nearby river for a forced landing on a sandbar. While descending to fly beneath a trestle bridge that was between his location and the sandbar, the airplane collided with a wire beneath the bridge. The airplane veered to the right, descended and impacted with "scrub trees/saplings" on a side of the river. The airplane was recovered. Postaccident, the airplane was inspected by a Federal Aviation Administration (FAA) certificated mechanic with inspection authorization (IA). Fuel flow testing was performed which revealed that with fuel supplied to the fuel tank and the flexible fuel line removed from the carburetor inlet, it took approximately 14 minutes to fill a gallon container. Continued testing revealed "rust" exited a hard aluminum fuel line between the outlet of the "header" tank to the inlet of the fuel shut-off valve. The lines were cleared and flow testing revealed it took approximately 2 minutes 4 seconds to fill a gallon container. Additionally, cold differential compression testing of each cylinder revealed no cylinder was greater than 52 psi when using 80 psi as a reference. A copy of the statement from the IA is an attachment to this report. The airplane was inspected last in accordance with an annual inspection on February 3, 2000; the pilot indicated that the airplane had accumulated approximately 20 hours since then at the time of the accident. No inspections were recorded between a periodic inspection on June 8, 1963, and an annual inspection December 12, 1994. The December 1994 entry indicates, "Assembled aircraft after long term storage...." There was no record of any fuel lines being replaced. Copies of maintenance records are an attachment to this report. The pilot flew to a nearby airport, landed, remained on the ground with the engine running, then elected to depart. During the initial climb about 50-100 feet agl, the engine experienced a loss of power. Unable to maintain altitude he maneuvered towards a sandbar in a river and while descending to fly beneath a trestle bridge that was between his location and the sandbar, the airplane collided with a wire beneath the bridge. The airplane veered to the right, descended and impacted with 'scrub trees/saplings' on a side of the river. Examination of the airplane revealed 'rust' from a fuel line between the header tank and the fuel shut-off valve. Removal of the rust revealed an increase in fuel flow to the carburetor. Cold differential compression testing of each cylinder revealed no cylinder was greater than 52 psi when using 80 psi as a reference. The last annual inspection occurred on February 3, 2000; the airplane had accumulated approximately 20 hours since then. No inspections were recorded between a periodic inspection on June 8, 1963, and an annual inspection December 12, 1994. The December 1994 entry indicates, 'Assembled aircraft after long term storage....' No record of fuel lines was noted. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_2000_MIA00LA220.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (fuel starvation, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗