NTSB CAROL · Event
Event CEN10LA482
Aircraft involved
Probable cause & findings
A total loss of engine power while on final approach for undetermined reasons.
Factual narrative
On August 13, 2010, about 1142 eastern daylight time, a Cessna T210M, N14AW, piloted by a private pilot, was substantially damaged during a forced landing following a loss of engine power. The airplane was on approach to Runway 3 at Put-in-Bay Airport (3W2), Put-in-Bay, Ohio, when the engine lost power. The pilot subsequently ditched into Lake Erie about 1/4 mile southwest of the runway, near the Miller Ferry dock. The personal flight was being conducted under 14 Code of Federal Regulations Part 91 without a flight plan. Visual meteorological conditions prevailed. The pilot and two passengers successfully evacuated the airplane without injury. The third passenger reported minor injuries. The flight departed from Canton-Plymouth-Mettetal Airport (1D2), Plymouth, Michigan, about 1105. The intended destination was 3W2. The pilot reported that he had initially entered the traffic pattern for runway 3 at 1D2. However, due to conflicts with other traffic, he elected to extend the base leg and continue in the pattern in order let the other traffic get organized. The remainder of the second traffic pattern for runway 3 was "uneventful" until he the engine "went silent" as he rolled out on final approach. The pilot noted that the engine lost power without "missing, stumbling or hesitating" and there seemed to be no signs of a mechanical problem. The propeller continued to windmill. His attempts to restore engine power were unsuccessful. The pilot subsequently ditched the airplane near a ferry dock on the south end of South Bass Island. The pilot and three passengers were rescued by a ferry boat. The airplane came to rest in about 22 feet of water, approximately 50 yards from the shoreline. It was recovered about 2000 that evening. The airframe had sustained substantial damage to the fuselage and empennage. The accident engine was a Teledyne Continental Motors TSIO-520-R9, serial number 294483-R. It was manufactured in July 2003 and installed on the accident airplane in April 2004. The recording tachometer indicated 4,674.9 hours at that time. According to the engine log, a "top overhaul" was completed on December 14, 2008, at 5,720.0 hours, which included overhaul of the cylinders and installation of new after market (non-OEM) intake and exhaust valves. An annual inspection had been completed on November 12, 2009, at 5,864.0 hours. The most recent maintenance consisted of an oil change and was completed on April 12, 2010. The engine time associated with that oil change was 5,910.0 hours. The pilot's logbook indicated a total flight time of 14.0 hours in the accident airplane between April 13, 2010, and the day of the accident. A post accident examination and operational test run of the engine did not reveal any anomalies consistent with a complete loss of engine power. A borescope examination of the #6 cylinder noted a section of missing material from the edge of the exhaust valve. The exhaust valve face exhibited an irregular combustion deposit pattern and the exterior of the cylinder was discolored in the area of the exhaust valve. These conditions are consistent with a leak at the exhaust valve during operation. Neither magneto produced a spark when operated on a test bench. Further examination revealed corroded carbon brush and contact point components on both units consistent with exposure to water. No other anomalies were observed. The oil filter element was removed; no contamination was observed. A new oil filter and operational magnetos were installed on the engine for a test run. The engine was not disassembled prior to the test run. The engine started normally and without hesitation. At full throttle, the engine operated at 2,250 rpm and 36.2 inches of mercury manifold pressure. The engine is rated for 2,700 rpm at 36.5 inches manifold pressure. A leak at the fuel control unit was observed during the test run. On disassembly, the o-rings sealing the unit did not return to their normal shape, but remained deformed. No other anomalies were observed with respect to the fuel control unit. According to the manufacturer, the component label appeared to pre-date the engine and the safety wire lead seal appeared consistent with a prior field overhaul of the unit. The pilot stated that the original fuel control unit had been replaced about two years prior to the accident. He did not recall noticing any sign of a fuel leak during operation of the airplane. The pilot reported he departed with approximately 16 gallons of fuel in both the left and right main tanks. Average fuel consumption for the accident airplane was about 15.2 gallons per hour, according to the pilot. The pilot reported that the engine experienced an abrupt loss of engine power while turning onto the final approach leg of the traffic pattern. His attempts to restore engine power were unsuccessful and he elected to ditch the airplane near a ferry dock. The airplane came to rest in about 22 feet of water, approximately 50 yards from the shoreline. A postaccident examination and operational test run of the engine did not reveal any anomalies consistent with a complete loss of engine power. The examination did reveal a section of missing material from the edge of the No. 6 cylinder exhaust valve and irregular combustion deposits on the face of the valve. Both signatures are consistent with an exhaust leak and a corresponding partial loss of engine power. During the test run, the engine started normally and without hesitation. The engine was unable to produce rated power due to an exhaust leak. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- C Aircraft-Aircraft power plant-Engine (reciprocating)-(general)-Not specified - C
- C Not determined-Not determined-(general)-(general)-Unknown/Not determined - C
- — Aircraft-Aircraft power plant-Engine (reciprocating)-Recip eng cyl section-Damaged/degraded
- — Aircraft-Aircraft power plant-Engine fuel and control-Fuel control/carburetor-Damaged/degraded
Verbatim from NTSB's published report. Source file
NTSB_2010_CEN10LA482.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (icing, stall, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
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Two-dimensional square ice in graphene nanocapillaries at room temperature is a fascinating phenomenon and has been confirmed experimentally.
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The Value of Strong Partnerships to Build a Successful Aviation Maintenance Career Pathway Program for Transitioning Military Service Members
The aerospace industry is competing with other industries for a qualified workforce, and many of those competing industries are investing heavily in creating workforce development pipelines.
- arXiv 2022 · arXiv preprint
Enhanced Prediction of Three-dimensional Finite Iced Wing Separated Flow Near Stall
Icing on three-dimensional wings causes severe flow separation near stall. Standard improved delayed detached eddy simulation (IDDES) is unable to correctly predict the separating reattaching flow due…
- NASA NTRS 2019 · Contractor Report (CR)
An Evaluation of an Analytical Simulation of an Airplane with Tailplane Icing by Comparison to Flight Data
This report presents the assessment of an analytical tool developed as part of the NASA/FAA Tailplane Icing Program. The analytical tool is a specialized simulation program called TAILSM4 which was de…
- NASA NTRS 2019 · Technical Publication (TP)
NASA/FAA Tailplane Icing Program: Flight Test Report
This report presents results from research flights that explored the characteristics of an ice-contaminated tailplane using various simulated ice shapes attached to the leading edge of the horizontal …
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