NTSB CAROL · Event
Event FTW71FQG56
Registry · N39067
FAA Aircraft Registry record.
Make / Model
LUSCOMBE 8E
Year of manufacture
1941 · 30 years old at event
Engine
LYCOMING 0-235 SERIES (115 hp)
Seats / Engines
2 seats · 1 engine
Last airworthiness date
19551008
ADS-B equipped
Yes — Mode-S A48613
Registrant of record
MILLER RONDO T
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Historical record (pre-1982)
NTSB recorded this accident in the pre-1982 coded-field schema — structured fields rather than free-text narrative. Decoded codes use established NTSB single-letter taxonomies; cause factors remain verbatim pending the Form 6120.4 codebook lookup.
Aircraft
LUSCOMBE 8E · N39067
Damage
Substantial
Craft type
Airplane
Classification
Accident
Light condition
Dawn
Weather
VMC
Phase of flight
Cruise — descent (EF)
Operator type
D
Airport
BROWN FIELD
Kind of flying
B0
Weather at impact
Sky
CLEAR
Aircraft history
Serial number
000000001828
Total time
1,325 hrs
Pilot
Certificate
Commercial — instrument
Total hours
144
Age
22
Investigator remarks
PLT RPTD HE HAD HIS HEELS ON THE BRAKE PEDALS.
Cause factors
- 64/A/22 A PILOT IN COMMAND IMPROPER OPERATION OF BRAKES AND/OR FLIGHT CONTROLS Cause — pilot/personnel action
Decoded against the NTSB Form 6120.4 cause-factor codebook (ct_Pre1982 table). Each row shows the raw triplet, modifier (Cause / Factor / etc.), category, and specific code.
Source: NTSB pre-1982 historical archive. Docket
3 0657.
Source file
NTSB_1971_3_0657.txt.
Modern CAROL record on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type. Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
- NASA NTRS 2019 · Conference Paper
Transonic Experimental Observations of Abrupt Wing Stall on an F/A-l8E Model
A transonic wind tunnel test of an 8% F/A-18E model was conducted in the NASA Langley Research Center (LaRC) 16 ft Transonic Tunnel (16-ft TT) to investigate on-surface flow physics during stall.
- NASA NTRS 2019 · Conference Paper
Transonic Experimental Observations of Abrupt Wing Stall on an F/A-18E Model (Invited)
A transonic wind tunnel test of an 8% F/A-18E model was conducted in the NASA Langley Research Center (LaRC) 16 ft Transonic Tunnel (16-ft TT) to investigate on-surface flow physics during stall.
Browse the full corpus — academia portal ↗