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Atlas / NTSB / LAX93LA062

NTSB CAROL · Event

Event LAX93LA062

1992-12-04 KAMUELA, Hawaii, United States Minor 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

THE INADEQUATE 100-HOUR INSPECTION PERFORMED BY COMPANY MAINTENANCE PERSONNEL. FACTORS CONTRIBUTING TO THIS ACCIDENT ARE THE FUEL CONTROL EXCEEDING THE MANUFACTURERS' SERVICE LIMITS; THE INOPERATIVE FUEL FILTER; THE OVERTEMPERATURE OF THE GAS GENERATOR TURBINE AND FREE TURBINE WHEELS; AND THE FALSE INDICATIONS OF THE TURBINE OUTLET TEMPERATURE INDICATOR.

Factual narrative

WHILE ON A SIGHTSEEING FLIGHT, THE HELICOPTER SUSTAINED A TOTAL LOSS OF POWER. THE PILOT EXECUTED AN AUTOROTATION TO A NEARBY ROAD. ON TOUCH DOWN THE HELICOPTER YAWED TO THE LEFT AND SKIDDED OFF THE ROAD BUCKLING THE LEFT SKID. THE ENGINE EXAMINATION DISCLOSED THAT THE TURBINE WHEELS SUSTAINED EXTENSIVE HIGH TEMPERATURE DISTRESS. THE FUEL CONTROL EXCEEDED ITS SERVICE LIMITS ON THE START AND ACCELERATION SCHEDULES. THE FUEL FILTER VALVE WAS FOUND IN THE BYPASS POSITION WITH ITS SPRING RUSTED AND THE VALVE SEAT CONTAINED DIRT PARTICLES. THE TURBINE OUTLET TEMPERATURE INDICATOR GAVE FALSE INDICATIONS, A LOWER THAN APPLIED TEMPERATURE, THROUGHOUT ITS OPERATIONAL PARAMETERS WHICH EXCEEDED THE SERVICABLE TOLERANCES. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1992_LAX93LA062.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗