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Atlas / NTSB / LAX94LA298

NTSB CAROL · Event

Event LAX94LA298

1994-07-26 CORONA, California, United States Airport · L66 Minor 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

AN UNDETERMINED PARTIAL LOSS OF ENGINE POWER.

Factual narrative

On July 26, 1994, at 2005 Pacific daylight time, a Grumman AA-1B, N8972L, operated by Paradise Aviation, Inc., experienced a partial loss of engine power during initial climb from runway 25 at the Corona Municipal (uncontrolled) Airport, Corona, California. The commercial pilot reported that he was unable to accelerate beyond the best angle of climb airspeed. After climbing to about 250 feet above the runway, the pilot entered a shallow bank turn to avoid colliding with trees. At the completion of the turn, the pilot attempted to reverse course and land on runway 07. Approaching the runway, the airplane descended into an open field and was substantially damaged. The pilot and passenger received minor injuries. Visual meteorological conditions prevailed at the time of the personal flight, and no flight plan was filed. The flight was originating at the time of the accident. The airplane was recovered from the accident site and was examined under the direction of the National Transportation Safety Board. No blockages were noted in the engine's induction system. The engine was test run. According to the mechanic who performed the test for the Safety Board, it ran extremely rough until the mixture control was pulled all the way out to idle cut off, at which time the engine smoothed out. The carburetor was visually inspected and no abnormalities were found. The throttle and mixture control linkages were reported to be correctly installed. ACCORDING TO THE PILOT, DURING INITIAL CLIMB HE EXPERIENCED A PARTIAL LOSS OF ENGINE POWER. THE PILOT ATTEMPTED TO MANEUVER THE AIRPLANE BACK TOWARD THE AIRPORT. INSUFFICIENT ENGINE POWER WAS PRODUCED TO SUSTAIN FLIGHT, AND THE AIRPLANE DESCENDED INTO ROUGH TERRAIN ABOUT 2 MILES FROM THE RUNWAY. FOLLOWING THE ACCIDENT, THE ENGINE WAS TEST RUN. THE ENGINE RAN ROUGH WITH THE MIXTURE CONTROL IN THE RICH POSITION, AND IT SMOOTHED OUT WHEN THE MIXTURE WAS PLACED IN THE LEAN POSITION. NO BLOCKAGES WERE NOTED IN THE ENGINE'S INDUCTION SYSTEM. THE CARBURETOR WAS VISUALLY INSPECTED AND NO ABNORMALITIES WERE FOUND. THE THROTTLE AND MIXTURE CONTROL LINKAGES WERE REPORTED TO BE CORRECTLY INSTALLED. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1994_LAX94LA298.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗