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Atlas / NTSB / MIA93LA149

NTSB CAROL · Event

Event MIA93LA149

1993-07-04 OCALA, Florida, United States Airport · OCF Minor 1 aircraft Status: Completed

Registry · N8962L

FAA Aircraft Registry record.

Make / Model

BOEING 737-8

Year of manufacture

2025

TCDS

A16WE · THE BOEING CO

Engine

CFM INTL LEAP-1B28 SER

Seats / Engines

175 seats · 2 engines

Last airworthiness date

20250620

ADS-B equipped

Yes — Mode-S AC5E47

Registrant of record

SOUTHWEST AIRLINES CO

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

PREMATURE LIFT OFF BY THE PILOT DURING TAKEOFF.

Factual narrative

On July 4, 1993, about 0906 eastern daylight time, a Grumman AA-1B, N8962L, registered to the pilot, William L. Hines, was substantially damaged during an aborted takeoff from the Ocala Municipal Airport, Ocala, Florida, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and no flight plan was filed for the local flight. The private pilot sustained minor injuries. The flight was originating at the time of the accident. The pilot stated that during the initial climb, the aircraft shuddered as if it would fall apart. The shuddering stopped after he decreased the angle of attack; and the engine did respond to throttle input. He again initiated a climb and the shuddering began again. He aborted the takeoff and while maneuvering to avoid obstacles at the departure end of the runway, the airplane stalled and landed hard on grass. The nose and right main landing gears collapsed. He further stated that the shuddering was similar to that encountered when performing stalls and that he did not hear any unusual engine sounds. As a result of the accident, the fuel tanks were damaged but the remaining fuel in them, the carburetor, and electric fuel pump were checked for water; none was found. A slight amount of sediment was found. An A & P mechanic who examined the engine stated that it was "intact." The magnetos were removed, rotated by hand, which revealed that they produced more than sufficient spark. THE FLIGHT DEPARTED AND DURING THE INITIAL CLIMB, THE PILOT REPORTED THAT THE AIRPLANE SHUDDERED AS IF IT WOULD FALL APART. THE SHUDDERING STOPPED WHEN HE DECREASED THE ANGLE OF ATTACK; AND THE ENGINE DID RESPOND TO THROTTLE INPUT. HE AGAIN INITIATED A CLIMB AND THE SHUDDERING STARTED AGAIN. HE ABORTED THE TAKEOFF AND WHILE MANEUVERING TO AVOID OBSTACLES PAST THE DEPARTURE END OF THE RUNWAY, THE AIRPLANE STALLED AND LANDED HARD ON THE GRASS. THE NOSE AND RIGHT MAIN LANDING GEARS COLLAPSED. HE FURTHER STATED THAT THE SHUDDERING WAS SIMILAR TO THAT ENCOUNTERED WHILE PERFORMING STALLS AND THAT HE DID NOT HEAR ANY UNUSUAL ENGINE SOUNDS. THE FUEL SYSTEM WAS CHECKED FOR WATER; NONE WAS FOUND. EXAMINATION OF THE ENGINE REVEALED NO EVIDENCE OF FAILURE OR MALFUNCTION. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1993_MIA93LA149.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗