NTSB CAROL · Event
Event SEA97FA202
Aircraft involved
Probable cause & findings
fatigue failure of the nose landing gear upper lock link, due in part to reduced strength after the manufacturing process was changed from forged to machined plate stock; and inadequate non-destructive inspection process for testing the link.
Factual narrative
HISTORY OF FLIGHT
On September 1, 1997, at 2110 Pacific daylight time, N951AS, a McDonnell-Douglas DC-9-82 (MD-82), operating as Alaska Airlines flight 255 from Los Angeles, California, to Seattle, Washington, sustained substantial damage when its nose landing gear collapsed during landing roll-out on runway 16L at Seattle-Tacoma International Airport. The two flight crewmembers and three flight attendants were uninjured. Seventeen of the 111 passengers incurred minor injuries during the emergency evacuation commanded by the captain after the airplane slid to a stop. There was no fire. According to the flight crewmembers, the airplane had departed Los Angeles, California with no indication of vibration or other abnormality. The flight was uneventful until the landing gear was extended and the nose landing gear warning light indicated an unsafe landing gear indication. At that time, the crew initiated a go-around (retracting the landing gear), climbed to a safe altitude in safe airspace, and then completed appropriate checklists in an attempt to obtain a safe gear-down indication with the landing gear extended. After completing appropriate checklists, the mechanical nose landing gear position indicator indicated that the nose landing gear was extended in a down and locked position, while the light continued to indicate an unsafe condition. The crew elected to land, and requested emergency equipment standing by. The captain stated that he landed the airplane smoothly; at about 60 knots indicated airspeed, the nose settled onto the runway and the airplane slid to a stop. The airplane slid about 1300 feet and drifted slightly to the right of centerline. He commanded an evacuation. All slides were deployed manually and the passengers evacuated quickly. During the course of recovering the airplane from the runway, it was determined that the nose landing gear upper lock link, part number 3914464-503, had failed, separating into two pieces. This item, which is subject to recurring non-destructive testing every 5000 cycles according to AD 97-02-10, had undergone an eddy current inspection 1075 cycles previous to the accident. This part was one of a series manufactured from plate stock, rather than being forged. Due to this changed process, according to the aircraft manufacturer, the lack of draft angle allowances on the machined parts reduced the load-carrying cross sectional area of the machined links to less than that of the forged links, resulting in a decrease in the overall strength. Metallurgical analysis revealed that approximately 10,000 major fatigue progression cycles had occurred within about .6 inches of the crack progression. Based upon the manufacturer's determination that there are two major stress cycles per gear retraction/extension cycle, the expected crack length 1075 cycles prior to the accident would have been greater than .25 inches. The Safety Board determined that there have been seven cracked or fractured upper lock links reported; all have RM serial numbers indicating that they came from Ready Machine, a now-defunct supplier to the airplane manufacturer.
INJURIES TO PERSONS
Nineteen individuals sustained minor injuries during the evacuation, including three with neck or back pain or spasms, some knee injuries, and one with a sprained ankle.
FLIGHT RECORDERS
The flight data recorder readout for the approach, landing, and landing rollout is attached.
WRECKAGE AND IMPACT INFORMATION
The airplane was inspected on-scene. The cockpit switches and controls were found to be secured. Their positions were not recorded. The cockpit crew side windows were open and the cockpit door was locked. During interviews, the flight crew noted that after calling for evacuation, they had evacuated out the cockpit windows. Damage included nose gear doors, skin scraping, and a wrinkled forward pressure bulkhead. During the course of on-scene investigation, it was noted that the jump seat at the mid-cabin flight attendant position was not retracted. The flight attendant at that duty station at the time of the accident noted that she did not notice that anomaly until after the evacuation was completed, and noted that it did not hamper the evacuation.
TESTS AND RESEARCH
The nose landing gear upper lock link, P/N 3914464-503, s/n RM 486, was analyzed by the material laboratory division of the NTSB. The metallurgist's factual report is attached. The inspection procedure and process provided by the airframe manufacturer does not specify removal of the upper lock link from the aircraft prior to recurring non-destructive tests (NDT). During the course of investigation, NTSB investigators and FAA inspectors observed that access to the upper lock link for NDT is limited when the part remains installed in the airplane.
ADDITIONAL INFORMATION
The aircraft was moved from the scene to the Alaska Airlines maintenance facility at SEATAC airport on the night of the accident. The Safety Board did not take possession of the wreckage. During the landing roll-out, the nose landing gear collapsed. Examination of the nose landing gear revealed the nose gear upper lock link, PN 3914464-503, had failed, and had separated into two pieces. The link, which was subject to recurring non-destructive testing every 5000 cycles (per AD 97-02-10), had an eddy current inspection by the operator, 1075 cycles before the accident. The link was one of a series manufactured from plate stock, rather than being forged. Due to this changed process, the lack of draft angle allowances on the machined parts reduced the load-carrying cross sectional area of the machined links to less than that of the forged links, resulting in a decrease in the overall strength. Metallurgical analysis revealed that about 10,000 major fatigue progression cycles had occurred within about .6 inches of the crack progression. Based on two major stress cycles per gear retraction/extension cycle, the crack length at 1075 cycles before the accident would have been greater than .25 inches. The inspection procedure and process provided by the airframe manufacturer did not specify removal of the upper lock link from the aircraft before recurring non-destructive tests (NDT). During the investigation, NTSB investigators and FAA inspectors observed that access to the upper lock link for NDT was limited when the part remained installed on the airplane. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_1997_SEA97FA202.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall, go-around, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
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