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Atlas / NTSB / WPR23LA196

NTSB CAROL · Event

Event WPR23LA196

2023-05-18 Seattle, Washington, United States Minor 1 aircraft Status: Completed

Registry · N2550L

FAA Aircraft Registry record.

Make / Model

CESSNA 172H

Engine

CONT MOTOR 0-300 SER (145 hp)

Seats / Engines

4 seats · 1 engine

ADS-B equipped

Yes — Mode-S A26C74

Registrant of record

WOOTEN CRAIG J

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

A stuck exhaust valve that resulted in a partial loss of engine power and a forced water ditching.

Factual narrative

On May 18, 2023, about 1817 Pacific daylight time, a Cessna 172H airplane, N2550L was substantially damaged when it was involved in an accident near Seattle, Washington. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot reported that, while in cruise flight at 1,000 ft msl nearing the destination airport, he heard an audible change in engine rpm. The engine tachometer indicated 1,400 rpm instead of the expected 2,000 rpm. There were no other abnormal engine sounds or indications on the instrument panel. The pilot attempted to troubleshoot; however, the engine rpm continued to decrease. No longer able to maintain altitude, the pilot declared an emergency and ditched the airplane into a bay, avoiding populated areas. A postaccident examination of the engine revealed the No. 4 cylinder exhaust valve was stuck in the partially open position. The intake valve was removed with little effort; however, the exhaust valve was removed with a punch and hammer along with significant force. The exhaust valve guide exhibited evidence of oil coking along with an area of polishing on one side of the guide. A slight amount of discoloration consistent with corrosion was observed adjacent to the polished area. The exhaust valve stem was intact with some coking near the valve fillet. The intake valve had moderate coking. The cooling fins on cylinder Nos. 2 and 4 exhibited thermal discoloration. All intake and exhaust valve springs were found intact and undamaged. The intake and exhaust pushrods were intact and undamaged. The No. 4 piston exhibited evidence of corrosion and combustion deposits were observed on the piston face. All piston rings were intact and had various degrees of corrosion and contamination throughout. The internal area of the crankcase, the camshaft, and crankshaft were found to be unremarkable. The aircraft maintenance logbook revealed that the engine had a major overhaul September 8, 1995. On March 16, 2022, the No. 4 cylinder was serviced and reinstalled with a new cylinder kit. The exhaust and intake valve guides were reamed, and the valves were reinstalled. At that time, the engine had accumulated 1,021.8 hours since major overhaul. The airplane had 143.2 total flight hours from the time of the No. 4 cylinder servicing until the accident and the engine had 1,165 total hours since new at the time of the accident. The airplane’s most recent annual inspection was completed on June 8, 2022. The annual inspection included replacement of the No. 4 cylinder exhaust stack. The engine manufacturer recommended overhaul time for the engine was 1,800 hours or 12 years, whichever occurred first. The pilot reported that, as the airplane descended to 1,000 ft mean sea level (msl) crossing over a bay, the engine sustained a partial loss of power. The pilot declared an emergency and performed a forced water ditching. Examination of the engine revealed a stuck exhaust valve on the No. 4 cylinder. The No. 4 cylinder was removed for further examination. The exhaust valve guide exhibited evidence of oil coking along with an area of polishing on one side of the guide. A slight amount of discoloration consistent with corrosion was observed adjacent to the polished area. The exhaust valve stem was intact with some coking near the valve fillet and the intake valve exhibited moderate coking. It is likely that the coking resulted in the valve getting stuck. The Nos. 2 and 4 cylinder cooling fins exhibited thermal discoloration. A visual inspection of the internal area of the crankcase showed the crankshaft and camshaft did not reveal any anomalies or mechanical damage. The No. 4 cylinder had been serviced and reinstalled with a new cylinder kit 143 flight hours before the accident and the most recent annual inspection was about 11 months before the accident. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Aircraft-Aircraft power plant-Engine (reciprocating)-Recip eng cyl section-Damaged/degraded
  • Aircraft-Aircraft power plant-Power plant-(general)-Related maintenance info

Verbatim from NTSB's published report. Source file NTSB_2023_WPR23LA196.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (icing, stall, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗