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Atlas / NTSB / CEN25LA102

NTSB CAROL · Event

Event CEN25LA102

2025-02-24 Iron River, Michigan, United States Airport · Y73 None 1 aircraft Status: Completed

Registry · N34284

FAA Aircraft Registry record.

Make / Model

CESSNA 177B

Year of manufacture

1972 · 53 years old at event

Engine

LYCOMING O&VO-360 SER (180 hp)

Seats / Engines

4 seats · 1 engine

Last airworthiness date

19721002

ADS-B equipped

Yes — Mode-S A3C849

Registrant of record

LADD MICHAEL

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The airplane’s collision with runway lights during takeoff due to reduced airplane climb performance. Contributing to the accident was the shifting winds during takeoff which likely developed into a tailwind.

Factual narrative

The pilot reported that before takeoff he calculated the airplane weight to be 104 lbs below maximum gross weight, the takeoff distance to be about 985 ft, and estimated the wind to be from 250° at 15 knots gusting to 30 knots. The pilot departed from runway 17 and rotated the airplane for takeoff about 1,250 ft down the 2,000 ft runway. He noted that the airplane did not climb as expected, and he kept the airplane wings level in ground effect, but the airplane drifted left and collided with the runway end lights. The pilot continued the initial climb and realized that the right main landing gear tire had separated from the airplane. He continued to his destination airport and landed on the runway without further incident. Postaccident examination of the airplane revealed substantial damage to the left horizontal stabilator. The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation. Following the accident, the pilot assessed that wind may have shifted to a tailwind resulting in a loss of airplane performance. The closest aviation weather reporting facility was 25 nautical miles from the departure airport which reported a variable wind from 260° to 320° at 14 knots gusting to 24 knots. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Personnel issues-Psychological-Attention/monitoring-Monitoring environment-Pilot
  • Environmental issues-Conditions/weather/phenomena-Wind-Tailwind-Effect on operation
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Climb rate-Not attained/maintained

Verbatim from NTSB's published report. Source file NTSB_2025_CEN25LA102.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type. Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗