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Atlas / NTSB / DEN04LA071

NTSB CAROL · Event

Event DEN04LA071

2004-05-08 Englewood, Colorado, United States Airport · KAPA Serious 1 aircraft Status: Completed

Registry · N185K

FAA Aircraft Registry record.

Make / Model

CESSNA A185E

Year of manufacture

1971 · 33 years old at event

Engine

CONT MOTOR IO 520 SERIES (285 hp)

Seats / Engines

6 seats · 1 engine

Last airworthiness date

19910621

ADS-B equipped

Yes — Mode-S A15420

Registrant of record

NORTHERN AVIATION LLC

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

the pilot's inadequate preflight planning which failed to verify an adequate fuel supply and his inadequate in-flight planning/decision which resulted in fuel exhaustion. The inadequate indication of his fuel quantity system is a contributing factor.

Factual narrative

On May 8, 2004, approximately 0915 mountain daylight time, a Cessna A185E, N185K, piloted by a private pilot, was substantially damaged when the engine lost power and it struck terrain 0.25 miles short of runway 17L at Centennial Airport (APA), Englewood, Colorado. Visual meteorological conditions prevailed at the time of the accident. The personal flight was being conducted under the provisions of Title 14 CFR Part 91 without a flight plan. The pilot received minor injuries, but his passenger was seriously injured. The flight originated at Everitt Airstrip, Parker, Colorado, approximately 0910, and was en route to Centennial Airport. In his accident report, the pilot stated that this was a "short nine (9) mile flight" to refuel. He had been cleared to land and was following "slow" traffic to runway 17L. He reduced airspeed and made a constant left turn. When he rolled out on final approach, he opened the throttle to arrest the descent rate. The engine did not respond although it was still running. He relaxed back pressure on the control yoke to maintain airspeed and banked slightly to land on a steep incline short of runway 17L. The descent rate increased and the airplane impacted the incline. Postaccident examination revealed the main landing gear was torn out of the fuselage, the firewall was buckled, and the forward portion of the fuselage aft of the firewall was wrinkled. On May 1, 2003, a Shaddin Fuel Flow system was installed in the airplane. The system digitally indicates, by the toggling of a switch, total fuel on board, consumption rate, endurance, and fuel remaining. The pilot said that prior to taking off from Everett, he checked the fuel quantity and it indicated 10.1 gallons. After the accident, he again checked the fuel quantity and it indicated 8.0 gallons. If properly installed and calibrated correctly, the system will indicate no more than a plus or minus 1.0 gallon error. The recovery crew said that when they retrieved the airplane, they drained only one gallon from the fuel tanks. The pilot said that several months before the accident, the bracket that secured the throttle cable to the firewall broke. This happened while the airplane was being taxied. Maintenance records contained no entry of a repair being made. Although the engine had been pushed aft and buckled the firewall, cockpit movement of the throttle produced cable movement at the throttle valve. The pilot had been cleared to land and was following slower traffic. He reduced airspeed and made a constant left turn. When he rolled out on final approach, he opened the throttle to arrest the descent rate. The engine did not respond although it was still running. He relaxed back pressure on the control yoke to maintain airspeed and banked slightly to land on a steep incline short of the runway. The descent rate increased and the airplane impacted the incline. Postaccident examination revealed the main landing gear was torn out of the fuselage, the firewall was buckled, and the forward portion of the fuselage aft of the firewall was wrinkled. One year earlier, a fuel management system was installed in the airplane. The system digitally indicates, by the toggling of a switch, total fuel on board, consumption rate, endurance, and fuel remaining. The pilot said that prior to taking off for the 8-mile flight, he checked the fuel quantity and it indicated 10.1 gallons. After the accident, he again checked the fuel quantity and it indicated 8.0 gallons. If properly installed and calibrated correctly, the system will indicated no more than a plus or minus 1.0 gallon error. The recovery crew drained one gallon from all the fuel tanks. The pilot said that several months before the accident, the bracket that secured the throttle cable to the firewall broke. Maintenance records contained no entry of a repair being made. Although the engine had been pushed aft and buckled the firewall, cockpit movement of the throttle produced cable movement at the throttle valve. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_2004_DEN04LA071.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall, fuel exhaustion, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗